In some cases ACPI control methods used during device enumeration
(such as _HID or _STA) may rely on Operation Region handlers
supplied by the drivers of other devices [1]:
An example of this is the Acer Switch 10E SW3-016 model. The _HID
method of the ACPI node for the UART attached Bluetooth, reads
GPIOs to detect the installed wifi chip and update the _HID for the
Bluetooth's ACPI node accordingly. The current ACPI scan code calls
_HID before the GPIO controller's OpRegions are available, leading
to the wrong _HID being used and Bluetooth not working.
In principle, in those cases there should be a _DEP control method
under the device object with OpRegion enumeration dependencies, so
deferring the enumeration of devices with _DEP returning a non-empty
list of suppliers of OpRegions depended on by the given device
(modulo some known exceptions that don't really supply any OpRegions
and are listed by _DEP for other reasons irrelevant for Linux) should
at least address the first-order dependencies by allowing the OpRegion
suppliers to be enumerated before their consumers.
Implement the above idea by modifying acpi_bus_scan() to enumerate
devices in the given scope of the ACPI namespace in two passes,
where the first pass covers the devices without "significant" lists
of dependencies coming from _DEP only and the second pass covers
all of the devices that were not enumerated in the first pass.
Take _DEP into account only for device objects with _HID, mostly in
order to avoid deferring the creation of ACPI device objects that
represent PCI devices and must be present during the enumeration
of the PCI bus (which takes place during the processing of the ACPI
device object that represents the host bridge), so that they can
be properly associated with the corresponding PCI devices.
Link: https://lore.kernel.org/linux-acpi/20201121203040.146252-1-hdegoede@redhat.com/ # [1]
Reported-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com>
Reviewed-by: Hans de Goede <hdegoede@redhat.com>
Tested-by: Hans de Goede <hdegoede@redhat.com>
Reviewed-by: Mika Westerberg <mika.westerberg@linux.intel.com>
Evaluate _DEP before calling acpi_add_single_object() from
acpi_bus_check_add() and do that only for ACPI_BUS_TYPE_DEVICE
objects.
While at it, rename acpi_device_dep_initialize() to
acpi_scan_check_dep(), fix up a memory allocation statement in
that function, consistently treat memory allocation failures in
there as intermittent errors and make some related janitorial
changes in it.
This change will help to avoid calling acpi_add_single_object() if
there are unmet _DEP dependencies in the future, as that may cause
some control methods, potentially depending on the presence of
operation regions supplied by other devices, to be evaluated
prematurely.
Signed-off-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com>
Reviewed-by: Hans de Goede <hdegoede@redhat.com>
Tested-by: Hans de Goede <hdegoede@redhat.com>
Reviewed-by: Mika Westerberg <mika.westerberg@linux.intel.com>
We don't need to take uring_lock for SQPOLL|IOPOLL to do
io_cqring_overflow_flush() when cq_overflow_list is empty, remove it
from the hot path.
Signed-off-by: Pavel Begunkov <asml.silence@gmail.com>
Signed-off-by: Jens Axboe <axboe@kernel.dk>
There is only one user of it and the name is misleading, get rid of it
by inlining. By the way make overflow_flush's return value deduction
simpler.
Signed-off-by: Pavel Begunkov <asml.silence@gmail.com>
Signed-off-by: Jens Axboe <axboe@kernel.dk>
Add a helper which calculates number of events in CQ. Handcoded version
of it in io_cqring_overflow_flush() is not the clearest thing, so it
makes it slightly more readable.
Signed-off-by: Pavel Begunkov <asml.silence@gmail.com>
Signed-off-by: Jens Axboe <axboe@kernel.dk>
list_empty_careful() is not racy only if some conditions are met, i.e.
no re-adds after del_init. io_cqring_overflow_flush() does list_move(),
so it's actually racy.
Remove those checks, we have ->cq_check_overflow for the fast path.
Signed-off-by: Pavel Begunkov <asml.silence@gmail.com>
Signed-off-by: Jens Axboe <axboe@kernel.dk>
io_uring_cancel_task_requests() doesn't imply that the ring is going
away, it may continue to work well after that. The problem is that it
sets ->cq_overflow_flushed effectively disabling the CQ overflow feature
Split setting cq_overflow_flushed from flush, and do the first one only
on exit. It's ok in terms of cancellations because there is a
io_uring->in_idle check in __io_cqring_fill_event().
It also fixes a race with setting ->cq_overflow_flushed in
io_uring_cancel_task_requests, whuch's is not atomic and a part of a
bitmask with other flags. Though, the only other flag that's not set
during init is drain_next, so it's not as bad for sane architectures.
Signed-off-by: Pavel Begunkov <asml.silence@gmail.com>
Fixes: 0f2122045b ("io_uring: don't rely on weak ->files references")
Signed-off-by: Jens Axboe <axboe@kernel.dk>
It will be helpful to trace the iocg's whole state, including active and
idle state. And we can easily expand the original iocost_iocg_activate
trace event to support a state trace class, including active and idle
state tracing.
Acked-by: Tejun Heo <tj@kernel.org>
Signed-off-by: Baolin Wang <baolin.wang@linux.alibaba.com>
Signed-off-by: Jens Axboe <axboe@kernel.dk>
The creation path of the NBD device respects max_part and only scans for
partitions if max_part is not 0. However, some other code paths ignore
max_part, and unconditionally scan for partitions. Add a check for
max_part on each partition scan.
Signed-off-by: Josh Triplett <josh@joshtriplett.org>
Reviewed-by: Josef Bacik <josef@toxicpanda.com>
Signed-off-by: Jens Axboe <axboe@kernel.dk>
The kernel doesn't seem to have clear rules around this, but various
spots are using the mmap_sem to serialize access to modifying the
locked_vm count. Play it safe and lock the mm for write when accounting
or unaccounting locked memory.
Signed-off-by: Jens Axboe <axboe@kernel.dk>
Commit d3817a6470 ("pwm: sun4i: Remove redundant needs_delay") changed
the logic of an else branch so that the PWM_EN and PWM_CLK_GATING bits
are now cleared if the PWM is to be disabled, whereas previously the
condition was always false, and hence the branch never got executed.
This code is reported causing backlight issues on boards based on the
Allwinner A20 SoC. Fix this by removing the else branch, which restores
the behaviour prior to the offending commit.
Note that the PWM_EN and PWM_CLK_GATING bits still get cleared later in
sun4i_pwm_apply() if the PWM is to be disabled.
Fixes: d3817a6470 ("pwm: sun4i: Remove redundant needs_delay")
Reported-by: Taras Galchenko <tpgalchenko@gmail.com>
Suggested-by: Taras Galchenko <tpgalchenko@gmail.com>
Tested-by: Taras Galchenko <tpgalchenko@gmail.com>
Reviewed-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
It is good practice to set the driver data before registering a device
with a subsystem because the subsystem or the driver core may call back
into the driver implementation. This is not currently an issue, but to
prevent future changes from causing this to break unexpectedly, make
sure that the driver data is set before the PWM chip registration.
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
This is only defined with CONFIG_PWM unset and was introduced together
with pwmchip_add_with_polarity() (which is only defined with CONFIG_PWM
enabled). I guess the series that introduced pwmchip_add_with_polarity()
had a different concept in earlier revisions and the !CONFIG_PWM part
was just not updated accordingly.
Given that there is no implementation for pwmchip_add_with_polarity()
without CONFIG_PWM, just drop pwmchip_add_inversed() instead of renaming
it to pwmchip_add_with_polarity().
Signed-off-by: Uwe Kleine-König <uwe@kleine-koenig.org>
Acked-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
The second parameter of do_div is an u32 and NSEC_PER_SEC * prescale
overflows this for bigger periods. Assuming the usual pwm input clk rate
of 66 MHz this happens starting at requested period > 606060 ns.
Splitting the division into two operations doesn't loose any precision.
It doesn't need to be feared that c / NSEC_PER_SEC doesn't fit into the
unsigned long variable "duty_cycles" because in this case the assignment
above to period_cycles would already have been overflowing as
period >= duty_cycle and then the calculation is moot anyhow.
Fixes: aef1a3799b ("pwm: imx27: Fix rounding behavior")
Signed-off-by: Uwe Kleine-König <uwe@kleine-koenig.org>
Tested-by: Johannes Pointner <johannes.pointner@br-automation.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Use the newer .apply function of pwm_ops instead of .config, .enable,
.disable and .set_polarity. This guarantees atomic changes of the pwm
controller configuration. It also reduces the size of the driver.
Since now period is a 64 bit value, add an extra check to reject periods
that exceed the possible max value for the 32 bit register.
This has been tested on a Raspberry PI 4.
Signed-off-by: Lino Sanfilippo <LinoSanfilippo@gmx.de>
Reviewed-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
The driver used this construct:
#define KMB_PWM_LEADIN_MASK GENMASK(30, 0)
static inline void keembay_pwm_update_bits(struct keembay_pwm *priv, u32 mask,
u32 val, u32 offset)
{
u32 buff = readl(priv->base + offset);
buff = u32_replace_bits(buff, val, mask);
writel(buff, priv->base + offset);
}
...
keembay_pwm_update_bits(priv, KMB_PWM_LEADIN_MASK, 0,
KMB_PWM_LEADIN_OFFSET(pwm->hwpwm));
With CONFIG_CC_OPTIMIZE_FOR_SIZE the compiler (here: gcc 10.2.0) this
triggers:
In file included from /home/uwe/gsrc/linux/drivers/pwm/pwm-keembay.c:16:
In function ‘field_multiplier’,
inlined from ‘keembay_pwm_update_bits’ at /home/uwe/gsrc/linux/include/linux/bitfield.h:124:17:
/home/uwe/gsrc/linux/include/linux/bitfield.h:119:3: error: call to ‘__bad_mask’ declared with attribute error: bad bitfield mask
119 | __bad_mask();
| ^~~~~~~~~~~~
In function ‘field_multiplier’,
inlined from ‘keembay_pwm_update_bits’ at /home/uwe/gsrc/linux/include/linux/bitfield.h:154:1:
/home/uwe/gsrc/linux/include/linux/bitfield.h:119:3: error: call to ‘__bad_mask’ declared with attribute error: bad bitfield mask
119 | __bad_mask();
| ^~~~~~~~~~~~
The compiler doesn't seem to be able to notice that with field being
0x3ffffff the expression
if ((field | (field - 1)) & ((field | (field - 1)) + 1))
__bad_mask();
can be optimized away.
So use __always_inline and document the problem in a comment to fix
this.
Reported-by: kernel test robot <lkp@intel.com>
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Tested-by: Vijayakannan Ayyathurai <vijayakannan.ayyathurai@intel.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Permission bits are easier readable in octal than with using the
symbolic names.
Fixes the following warning generated by checkpatch:
WARNING: Symbolic permissions 'S_IRUGO' are not preferred. Consider using octal permissions '0444'.
#1341: FILE: drivers/pwm/core.c:1341:
+ debugfs_create_file("pwm", S_IFREG | S_IRUGO, NULL, NULL,
Signed-off-by: Soham Biswas <sohambiswas41@gmail.com>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
All used ACPI functions have dummy implementations, and there is no hard
dependency on x86.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Drivers making use of IO remapping must depend on HAS_IOMEM.
Reported-by: kernel test robot <lkp@intel.com>
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Instead of using a mix of -EOPNOTSUPP and -ENOTSUPP, use the more
standard -EINVAL to signal that the specified polarity value was
invalid.
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
A single blank line is enough to separate logical code blocks.
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Using gotos for conditional code complicates this code significantly.
Convert the code to simple conditional blocks to increase readability.
Suggested-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Intel Lightning Mountain(LGM) SoC contains a PWM fan controller. This
PWM controller does not have any other consumer, it is a dedicated PWM
controller for fan attached to the system. Add driver for this PWM fan
controller.
Signed-off-by: Rahul Tanwar <rahul.tanwar@linux.intel.com>
Reviewed-by: Andy Shevchenko <andriy.shevchenko@intel.com>
Reviewed-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Intel's LGM(Lightning Mountain) SoC contains a PWM fan controller
which is only used to control the fan attached to the system. This
PWM controller does not have any other consumer other than fan.
Add DT bindings documentation for this PWM fan controller.
Signed-off-by: Rahul Tanwar <rahul.tanwar@linux.intel.com>
Reviewed-by: Rob Herring <robh@kernel.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Introduce driver for Synopsys DesignWare PWM Controller used on Intel
Elkhart Lake.
Initial implementation is done by Felipe Balbi while he was working at
Intel with later changes from Raymond Tan and me.
Co-developed-by: Felipe Balbi (Intel) <balbi@kernel.org>
Signed-off-by: Felipe Balbi (Intel) <balbi@kernel.org>
Co-developed-by: Raymond Tan <raymond.tan@intel.com>
Signed-off-by: Raymond Tan <raymond.tan@intel.com>
Signed-off-by: Jarkko Nikula <jarkko.nikula@linux.intel.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Add binding for MT8167 SoC. The IP is compatible with MT8173.
Signed-off-by: Fabien Parent <fparent@baylibre.com>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Rob Herring <robh@kernel.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
The MediaTek PWM IP can sometimes use the 26 MHz source clock to
generate the PWM signal, but the driver currently assumes that we always
use the PWM bus clock to generate the PWM signal.
This commit modifies the PWM driver in order to force the PWM IP to
always use the bus clock as source clock.
I do not have the datasheet of all the MediaTek SoC, so I don't know if
the register to choose the source clock is present in all the SoCs or
only in subset. As a consequence I made this change optional by using a
platform data paremeter to says whether this register is supported or
not. On all the SoCs I don't have the datasheet (MT2712, MT7622, MT7623,
MT7628, MT7629) I kept the behavior to be the same as before this
change.
Signed-off-by: Fabien Parent <fparent@baylibre.com>
Reviewed-by: Matthias Brugger <matthias.bgg@gmail.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
When there are other PWM controllers enabled along with pwm-lp3943,
pwm-lp3942 is failing to probe with -EEXIST error. This is because
other PWM controllers are probed first and assigned PWM base 0 and
pwm-lp3943 is requesting for 0 again.
In order to avoid this, assign the chip base with -1, so that it is
dynamically allocated.
Fixes: af66b3c093 ("pwm: Add LP3943 PWM driver")
Signed-off-by: Lokesh Vutla <lokeshvutla@ti.com>
Reviewed-by: Uwe Kleine-König <u.kleine-könig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Add sama5d2 support. The sama5d2 has a new clock input, its gclk. Index 0
of the clock selector is the gclk instead of the peripheral clock divided
by 2.
For now, the gclk is not used because the peripheral clock divided by 8
already gives a 9.6ns resolution which is enough for most use cases.
Signed-off-by: Alexandre Belloni <alexandre.belloni@bootlin.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
The PWM is now a subnode of the used TCB. This is cleaner and it mainly
allows to stop wasting TCB channels when only 2 or 4 PWMs are used.
This also removes the atmel_tclib dependency
Cc: Thierry Reding <thierry.reding@gmail.com>
Cc: linux-pwm@vger.kernel.org
Signed-off-by: Alexandre Belloni <alexandre.belloni@bootlin.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Move the TCB pwm nodes under their parent. This removes the need for the
tc-block property as there is now a child-parent relationship between the
TC channel and the TC block.
Move the documentation to the main file.
Signed-off-by: Alexandre Belloni <alexandre.belloni@bootlin.com>
Reviewed-by: Rob Herring <robh@kernel.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
The devm_clk_get() may return -EPROBE_DEFER which is not handled properly
by TI EHRPWM driver and causes unnecessary boot log messages.
Hence, add proper deferred probe handling with new dev_err_probe() API.
Signed-off-by: Grygorii Strashko <grygorii.strashko@ti.com>
Reviewed-by: Vignesh Raghavendra <vigneshr@ti.com>
Reviewed-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
As the comment above the code setting the DPM_FLAG_NO_DIRECT_COMPLETE
flag explains:
/*
* On Cherry Trail devices the GFX0._PS0 AML checks if the controller
* is on and if it is not on it turns it on and restores what it
* believes is the correct state to the PWM controller.
* Because of this we must disallow direct-complete, which keeps the
* controller (runtime)suspended, on resume to avoid 2 issues:
* 1. The controller getting turned on without the linux-pm code
* knowing about this. On devices where the controller is unused
* this causes it to stay on during the next suspend causing high
* battery drain (because S0i3 is not reached)
* 2. The state restoring code unexpectedly messing with the controller
*/
The pm-core must not skip resume to avoid the GFX0._PS0 AML code messing
with the PWM controller behind our back. But leaving the controller
runtime-suspended (skipping runtime-resume + normal-suspend) during
suspend is fine. Set the DPM_FLAG_SMART_SUSPEND flag to allow this.
Reviewed-by: Andy Shevchenko <andy.shevchenko@gmail.com>
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
ACPI LPSS devices use direct-complete style suspend/resume handling by
default. We set the DPM_FLAG_SMART_PREPARE and define a prepare handler
to disable this on Cherry Trail devices.
Clean this up a bit by setting the DPM_FLAG_NO_DIRECT_COMPLETE flag for
Cherry Trail devices, instead of defining a prepare handler.
While at it also improve the comment explaining why this is necessary.
Reviewed-by: Andy Shevchenko <andy.shevchenko@gmail.com>
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
pwm_lpss_is_updating() does a sanity check which should never fail.
If the check does actually fail that is worth logging an error,
especially since this means that we will skip making the requested
changes to the PWM settings.
Reviewed-by: Andy Shevchenko <andy.shevchenko@gmail.com>
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
The ab8500 driver is the last one which doesn't (explicitly) use dynamic
allocation of the pwm id. Looking through the kernel sources I didn't
find a place that relies on this id. And with the device probed from
device tree pdev->id is -1 anyhow; making this explicit looks
beneficial, too.
Signed-off-by: Uwe Kleine-König <uwe@kleine-koenig.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
pwmchip_add() doesn't emit an error message, so add one in the driver.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
dev_err_probe() can reduce code size, uniform error handling and record the
defer probe reason etc., use it to simplify the code.
Signed-off-by: Anson Huang <Anson.Huang@nxp.com>
Acked-by: Lee Jones <lee.jones@linaro.org>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
dev_err_probe() can reduce code size, uniform error handling and record the
defer probe reason etc., use it to simplify the code.
Signed-off-by: Anson Huang <Anson.Huang@nxp.com>
Acked-by: Lee Jones <lee.jones@linaro.org>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
dev_err_probe() can reduce code size, uniform error handling and record the
defer probe reason etc., use it to simplify the code.
Signed-off-by: Anson Huang <Anson.Huang@nxp.com>
Acked-by: Lee Jones <lee.jones@linaro.org>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Use devm_platform_ioremap_resource() to simplify code. While at it, also
declare the "i" and "ret" variables on the same line since they are of
the same type.
Signed-off-by: Yangtao Li <tiny.windzz@gmail.com>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Reviewed-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>