There is no call to i2c_get_clientdata(), platform_get_drvdata(),
or dev_get_drvdata() in any of the drivers in this patch.
Signed-off-by: Guenter Roeck <linux@roeck-us.net>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
max7359_build_keycode() does the same thing as matrix_keypad_build_keymap(),
but the latter can also handle DT bindings.
Tested on beagleboard-xm.
Signed-off-by: Evgeniy A. Dushistov <dushistov@mail.ru>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
In datasheet of max7359 there is the following description of this flag:
0 - INT cleared when FIFO empty,
1 - INT cleared after host read. In this mode, I2C should read
FIFO until interrupt condition removed, or further INT may be lost.
So, if we set this flag, we have to read FIFO until it becomes empty. But
in interrupt we read FIFO just once. This lead to "keyboard" hang until
reboot, if we press several keys, because of interrupt handler read just
one "press" from FIFO and clear interrupt.
Signed-off-by: Evgeniy A. Dushistov <dushistov@mail.ru>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
This patch introduces the use of managed interfaces like devm_kzalloc,
devm_input_allocate_device, devm_request_threaded_irq etc. and does away
with the calls to free the allocated memory. The remove function is no
longer required and is completely done away with. Also, the labels in the
probe function are removed.
Signed-off-by: Himangi Saraogi <himangi774@gmail.com>
Acked-by: Julia Lawall <julia.lawall@lip6.fr>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Use the wrapper function for retrieving the platform data instead
of accessing dev->platform_data directly. This is a cosmetic change
to make the code simpler and enhance the readability.
Signed-off-by: Jingoo Han <jg1.han@samsung.com>
Acked-by: Fugang Duan <B38611@freescale.com>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Add CONFIG_PM_SLEEP to suspend/resume functions to fix the build
warnings when CONFIG_PM_SLEEP is not selected. This is because
sleep PM callbacks defined by SET_SYSTEM_SLEEP_PM_OPS are only used
when the CONFIG_PM_SLEEP is enabled.
drivers/input/keyboard/max7359_keypad.c:275:12: warning: 'max7359_suspend' defined but not used [-Wunused-function]
drivers/input/keyboard/max7359_keypad.c:287:12: warning: 'max7359_resume' defined but not used [-Wunused-function]
Signed-off-by: Jingoo Han <jg1.han@samsung.com>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
CONFIG_HOTPLUG is going away as an option so __devexit is no
longer needed.
Signed-off-by: Bill Pemberton <wfp5p@virginia.edu>
Acked-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
CONFIG_HOTPLUG is going away as an option so __devinit is no longer
needed.
Signed-off-by: Bill Pemberton <wfp5p@virginia.edu>
Acked-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Acked-by: Javier Martinez Canillas <javier@dowhile0.org>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
CONFIG_HOTPLUG is going away as an option so __devexit_p is no longer
needed.
Signed-off-by: Bill Pemberton <wfp5p@virginia.edu>
Acked-by: Russell King <rmk+kernel@arm.linux.org.uk>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
This patch converts the drivers in drivers/input/* to use the
module_i2c_driver() macro which makes the code smaller and a bit
simpler.
Signed-off-by: Axel Lin <axel.lin@gmail.com>
Signed-off-by: Dmitry Torokhov <dtor@mail.ru>
There is a general move to convert drivers to use dev_pm_ops rather than
bus specific ops to facilitate core work. Do this conversion for max7359.
Signed-off-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Signed-off-by: Dmitry Torokhov <dtor@mail.ru>
I2C drivers can use the clientdata-pointer to point to private data. As I2C
devices are not really unregistered, but merely detached from their driver, it
used to be the drivers obligation to clear this pointer during remove() or a
failed probe(). As a couple of drivers forgot to do this, it was agreed that it
was cleaner if the i2c-core does this clearance when appropriate, as there is
no guarantee for the lifetime of the clientdata-pointer after remove() anyhow.
This feature was added to the core with commit
e4a7b9b04d to fix the faulty drivers.
As there is no need anymore to clear the clientdata-pointer, remove all current
occurrences in the drivers to simplify the code and prevent confusion.
Signed-off-by: Wolfram Sang <w.sang@pengutronix.de>
Acked-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Acked-by: Greg Kroah-Hartman <gregkh@suse.de>
Acked-by: Richard Purdie <rpurdie@linux.intel.com>
Acked-by: Dmitry Torokhov <dtor@mail.ru>
Signed-off-by: Jean Delvare <khali@linux-fr.org>
percpu.h is included by sched.h and module.h and thus ends up being
included when building most .c files. percpu.h includes slab.h which
in turn includes gfp.h making everything defined by the two files
universally available and complicating inclusion dependencies.
percpu.h -> slab.h dependency is about to be removed. Prepare for
this change by updating users of gfp and slab facilities include those
headers directly instead of assuming availability. As this conversion
needs to touch large number of source files, the following script is
used as the basis of conversion.
http://userweb.kernel.org/~tj/misc/slabh-sweep.py
The script does the followings.
* Scan files for gfp and slab usages and update includes such that
only the necessary includes are there. ie. if only gfp is used,
gfp.h, if slab is used, slab.h.
* When the script inserts a new include, it looks at the include
blocks and try to put the new include such that its order conforms
to its surrounding. It's put in the include block which contains
core kernel includes, in the same order that the rest are ordered -
alphabetical, Christmas tree, rev-Xmas-tree or at the end if there
doesn't seem to be any matching order.
* If the script can't find a place to put a new include (mostly
because the file doesn't have fitting include block), it prints out
an error message indicating which .h file needs to be added to the
file.
The conversion was done in the following steps.
1. The initial automatic conversion of all .c files updated slightly
over 4000 files, deleting around 700 includes and adding ~480 gfp.h
and ~3000 slab.h inclusions. The script emitted errors for ~400
files.
2. Each error was manually checked. Some didn't need the inclusion,
some needed manual addition while adding it to implementation .h or
embedding .c file was more appropriate for others. This step added
inclusions to around 150 files.
3. The script was run again and the output was compared to the edits
from #2 to make sure no file was left behind.
4. Several build tests were done and a couple of problems were fixed.
e.g. lib/decompress_*.c used malloc/free() wrappers around slab
APIs requiring slab.h to be added manually.
5. The script was run on all .h files but without automatically
editing them as sprinkling gfp.h and slab.h inclusions around .h
files could easily lead to inclusion dependency hell. Most gfp.h
inclusion directives were ignored as stuff from gfp.h was usually
wildly available and often used in preprocessor macros. Each
slab.h inclusion directive was examined and added manually as
necessary.
6. percpu.h was updated not to include slab.h.
7. Build test were done on the following configurations and failures
were fixed. CONFIG_GCOV_KERNEL was turned off for all tests (as my
distributed build env didn't work with gcov compiles) and a few
more options had to be turned off depending on archs to make things
build (like ipr on powerpc/64 which failed due to missing writeq).
* x86 and x86_64 UP and SMP allmodconfig and a custom test config.
* powerpc and powerpc64 SMP allmodconfig
* sparc and sparc64 SMP allmodconfig
* ia64 SMP allmodconfig
* s390 SMP allmodconfig
* alpha SMP allmodconfig
* um on x86_64 SMP allmodconfig
8. percpu.h modifications were reverted so that it could be applied as
a separate patch and serve as bisection point.
Given the fact that I had only a couple of failures from tests on step
6, I'm fairly confident about the coverage of this conversion patch.
If there is a breakage, it's likely to be something in one of the arch
headers which should be easily discoverable easily on most builds of
the specific arch.
Signed-off-by: Tejun Heo <tj@kernel.org>
Guess-its-ok-by: Christoph Lameter <cl@linux-foundation.org>
Cc: Ingo Molnar <mingo@redhat.com>
Cc: Lee Schermerhorn <Lee.Schermerhorn@hp.com>
Convert max7359 driver to use IRQ threading instead of using
workqueue.
Tested-by: Joonyoung Shim <jy0922.shim@samsung.com>
Signed-off-by: Dmitry Torokhov <dtor@mail.ru>
The Maxim MAX7359 is a I2C interfaced key switch controller which
provides microprocessors with management of up to 64 key switches.
This patch adds support for the MAX7359 key switch controller.
Signed-off-by: Kim Kyuwon <q1.kim@samsung.com>
Reviewed-by: Trilok Soni <soni.trilok@gmail.com>
Signed-off-by: Dmitry Torokhov <dtor@mail.ru>