From 4fd6b5735c03c0955d93960d31f17d7144f5578f Mon Sep 17 00:00:00 2001
From: Robin Gong <yibin.gong@nxp.com>
Date: Fri, 22 May 2020 18:44:50 +0800
Subject: [PATCH 1/9] arm64: dts: imx8mm-evk: correct ldo1/ldo2 voltage range

Correct ldo1 voltage range from wrong high group(3.0V~3.3V) to low group
(1.6V~1.9V) because the ldo1 should be 1.8V. Actually, two voltage groups
have been supported at bd718x7-regulator driver, hence, just corrrect the
voltage range to 1.6V~3.3V. For ldo2@0.8V, correct voltage range too.
Otherwise, ldo1 would be kept @3.0V and ldo2@0.9V which violate i.mx8mm
datasheet as the below warning log in kernel:

[    0.995524] LDO1: Bringing 1800000uV into 3000000-3000000uV
[    0.999196] LDO2: Bringing 800000uV into 900000-900000uV

Fixes: 78cc25fa265d ("arm64: dts: imx8mm-evk: Add BD71847 PMIC")
Cc: stable@vger.kernel.org
Signed-off-by: Robin Gong <yibin.gong@nxp.com>
Reviewed-by: Dong Aisheng <aisheng.dong@nxp.com>
Reviewed-by: Fabio Estevam <festevam@gmail.com>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 arch/arm64/boot/dts/freescale/imx8mm-evk.dts | 4 ++--
 1 file changed, 2 insertions(+), 2 deletions(-)

diff --git a/arch/arm64/boot/dts/freescale/imx8mm-evk.dts b/arch/arm64/boot/dts/freescale/imx8mm-evk.dts
index e5ec8322796d..0f1d7f8aeac4 100644
--- a/arch/arm64/boot/dts/freescale/imx8mm-evk.dts
+++ b/arch/arm64/boot/dts/freescale/imx8mm-evk.dts
@@ -208,7 +208,7 @@
 
 			ldo1_reg: LDO1 {
 				regulator-name = "LDO1";
-				regulator-min-microvolt = <3000000>;
+				regulator-min-microvolt = <1600000>;
 				regulator-max-microvolt = <3300000>;
 				regulator-boot-on;
 				regulator-always-on;
@@ -216,7 +216,7 @@
 
 			ldo2_reg: LDO2 {
 				regulator-name = "LDO2";
-				regulator-min-microvolt = <900000>;
+				regulator-min-microvolt = <800000>;
 				regulator-max-microvolt = <900000>;
 				regulator-boot-on;
 				regulator-always-on;

From cfb12c8952f617df58d73d24161e539a035d82b0 Mon Sep 17 00:00:00 2001
From: Robin Gong <yibin.gong@nxp.com>
Date: Fri, 22 May 2020 18:44:51 +0800
Subject: [PATCH 2/9] arm64: dts: imx8mn-ddr4-evk: correct ldo1/ldo2 voltage
 range

Correct ldo1 voltage range from wrong high group(3.0V~3.3V) to low group
(1.6V~1.9V) because the ldo1 should be 1.8V. Actually, two voltage groups
have been supported at bd718x7-regulator driver, hence, just corrrect the
voltage range to 1.6V~3.3V. For ldo2@0.8V, correct voltage range too.
Otherwise, ldo1 would be kept @3.0V and ldo2@0.9V which violate i.mx8mn
datasheet as the below warning log in kernel:

[    0.995524] LDO1: Bringing 1800000uV into 3000000-3000000uV
[    0.999196] LDO2: Bringing 800000uV into 900000-900000uV

Fixes: 3e44dd09736d ("arm64: dts: imx8mn-ddr4-evk: Add rohm,bd71847 PMIC support")
Cc: stable@vger.kernel.org
Signed-off-by: Robin Gong <yibin.gong@nxp.com>
Reviewed-by: Dong Aisheng <aisheng.dong@nxp.com>
Reviewed-by: Fabio Estevam <festevam@gmail.com>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 arch/arm64/boot/dts/freescale/imx8mn-ddr4-evk.dts | 4 ++--
 1 file changed, 2 insertions(+), 2 deletions(-)

diff --git a/arch/arm64/boot/dts/freescale/imx8mn-ddr4-evk.dts b/arch/arm64/boot/dts/freescale/imx8mn-ddr4-evk.dts
index d07e0e6a00cc..a1e5483dbbbe 100644
--- a/arch/arm64/boot/dts/freescale/imx8mn-ddr4-evk.dts
+++ b/arch/arm64/boot/dts/freescale/imx8mn-ddr4-evk.dts
@@ -113,7 +113,7 @@
 
 			ldo1_reg: LDO1 {
 				regulator-name = "LDO1";
-				regulator-min-microvolt = <3000000>;
+				regulator-min-microvolt = <1600000>;
 				regulator-max-microvolt = <3300000>;
 				regulator-boot-on;
 				regulator-always-on;
@@ -121,7 +121,7 @@
 
 			ldo2_reg: LDO2 {
 				regulator-name = "LDO2";
-				regulator-min-microvolt = <900000>;
+				regulator-min-microvolt = <800000>;
 				regulator-max-microvolt = <900000>;
 				regulator-boot-on;
 				regulator-always-on;

From e353b325948d04f1305a7b4ad32eca87ba0823a2 Mon Sep 17 00:00:00 2001
From: Adam Ford <aford173@gmail.com>
Date: Tue, 26 May 2020 12:09:39 -0500
Subject: [PATCH 3/9] arm64: dts: imx8mm-beacon: Fix voltages on LDO1 and LDO2

LDO1 and LDO2 settings are wrong and case the voltage to go above the
maximum level of 2.15V permitted by the SoC to 3.0V.

This patch is based on work done on the i.MX8M Mini-EVK which utilizes
the same fix.

Fixes: 593816fa2f35 ("arm64: dts: imx: Add Beacon i.MX8m-Mini development kit")
Signed-off-by: Adam Ford <aford173@gmail.com>
Reviewed-by: Daniel Baluta <daniel.baluta@nxp.com>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 arch/arm64/boot/dts/freescale/imx8mm-beacon-som.dtsi | 4 ++--
 1 file changed, 2 insertions(+), 2 deletions(-)

diff --git a/arch/arm64/boot/dts/freescale/imx8mm-beacon-som.dtsi b/arch/arm64/boot/dts/freescale/imx8mm-beacon-som.dtsi
index fb0137a8611c..94911b1707ef 100644
--- a/arch/arm64/boot/dts/freescale/imx8mm-beacon-som.dtsi
+++ b/arch/arm64/boot/dts/freescale/imx8mm-beacon-som.dtsi
@@ -136,7 +136,7 @@
 
 			ldo1_reg: LDO1 {
 				regulator-name = "LDO1";
-				regulator-min-microvolt = <3000000>;
+				regulator-min-microvolt = <1600000>;
 				regulator-max-microvolt = <3300000>;
 				regulator-boot-on;
 				regulator-always-on;
@@ -144,7 +144,7 @@
 
 			ldo2_reg: LDO2 {
 				regulator-name = "LDO2";
-				regulator-min-microvolt = <900000>;
+				regulator-min-microvolt = <800000>;
 				regulator-max-microvolt = <900000>;
 				regulator-boot-on;
 				regulator-always-on;

From 04a2c05179b732a4c097f0a9c701ef4c9a37e1e3 Mon Sep 17 00:00:00 2001
From: Frieder Schrempf <frieder.schrempf@kontron.de>
Date: Thu, 28 May 2020 14:43:42 +0000
Subject: [PATCH 4/9] ARM: dts: imx6ul-kontron: Move watchdog from Kontron
 i.MX6UL/ULL board to SoM

The watchdog's WDOG_ANY signal is used to trigger a POR of the SoC,
if a soft reset is issued. As the SoM hardware connects the WDOG_ANY
and the POR signals, the watchdog node itself and the pin
configuration should be part of the common SoM devicetree.
Let's move it from the baseboard's devicetree to its proper place.

Fixes: 1ea4b76cdfde ("ARM: dts: imx6ul-kontron-n6310: Add Kontron i.MX6UL N6310 SoM and boards")
Cc: stable@vger.kernel.org
Signed-off-by: Frieder Schrempf <frieder.schrempf@kontron.de>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 arch/arm/boot/dts/imx6ul-kontron-n6x1x-s.dtsi       | 13 -------------
 .../boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi   | 13 +++++++++++++
 2 files changed, 13 insertions(+), 13 deletions(-)

diff --git a/arch/arm/boot/dts/imx6ul-kontron-n6x1x-s.dtsi b/arch/arm/boot/dts/imx6ul-kontron-n6x1x-s.dtsi
index f05e91841202..53a25fba34f6 100644
--- a/arch/arm/boot/dts/imx6ul-kontron-n6x1x-s.dtsi
+++ b/arch/arm/boot/dts/imx6ul-kontron-n6x1x-s.dtsi
@@ -232,13 +232,6 @@
 	status = "okay";
 };
 
-&wdog1 {
-	pinctrl-names = "default";
-	pinctrl-0 = <&pinctrl_wdog>;
-	fsl,ext-reset-output;
-	status = "okay";
-};
-
 &iomuxc {
 	pinctrl-0 = <&pinctrl_reset_out &pinctrl_gpio>;
 
@@ -409,10 +402,4 @@
 			MX6UL_PAD_NAND_DATA03__USDHC2_DATA3	0x170f9
 		>;
 	};
-
-	pinctrl_wdog: wdoggrp {
-		fsl,pins = <
-			MX6UL_PAD_GPIO1_IO09__WDOG1_WDOG_ANY	0x30b0
-		>;
-	};
 };
diff --git a/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi b/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi
index a17af4d9bfdf..fc316408721d 100644
--- a/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi
+++ b/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi
@@ -57,6 +57,13 @@
 	status = "okay";
 };
 
+&wdog1 {
+	pinctrl-names = "default";
+	pinctrl-0 = <&pinctrl_wdog>;
+	fsl,ext-reset-output;
+	status = "okay";
+};
+
 &iomuxc {
 	pinctrl-names = "default";
 	pinctrl-0 = <&pinctrl_reset_out>;
@@ -106,4 +113,10 @@
 			MX6UL_PAD_SNVS_TAMPER9__GPIO5_IO09      0x1b0b0
 		>;
 	};
+
+	pinctrl_wdog: wdoggrp {
+		fsl,pins = <
+			MX6UL_PAD_GPIO1_IO09__WDOG1_WDOG_ANY    0x30b0
+		>;
+	};
 };

From d22a16cc92e04d053fd807ef3587e4f135e4206f Mon Sep 17 00:00:00 2001
From: Frieder Schrempf <frieder.schrempf@kontron.de>
Date: Thu, 28 May 2020 14:43:43 +0000
Subject: [PATCH 5/9] ARM: dts: imx6ul-kontron: Change WDOG_ANY signal from
 push-pull to open-drain

The WDOG_ANY signal is connected to the RESET_IN signal of the SoM
and baseboard. It is currently configured as push-pull, which means
that if some external device like a programmer wants to assert the
RESET_IN signal by pulling it to ground, it drives against the high
level WDOG_ANY output of the SoC.

To fix this we set the WDOG_ANY signal to open-drain configuration.
That way we make sure that the RESET_IN can be asserted by the
watchdog as well as by external devices.

Fixes: 1ea4b76cdfde ("ARM: dts: imx6ul-kontron-n6310: Add Kontron i.MX6UL N6310 SoM and boards")
Cc: stable@vger.kernel.org
Signed-off-by: Frieder Schrempf <frieder.schrempf@kontron.de>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi | 2 +-
 1 file changed, 1 insertion(+), 1 deletion(-)

diff --git a/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi b/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi
index fc316408721d..61ba21a605a8 100644
--- a/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi
+++ b/arch/arm/boot/dts/imx6ul-kontron-n6x1x-som-common.dtsi
@@ -116,7 +116,7 @@
 
 	pinctrl_wdog: wdoggrp {
 		fsl,pins = <
-			MX6UL_PAD_GPIO1_IO09__WDOG1_WDOG_ANY    0x30b0
+			MX6UL_PAD_GPIO1_IO09__WDOG1_WDOG_ANY    0x18b0
 		>;
 	};
 };

From c95c9693b112f312b59c5d100fd09a1349970fab Mon Sep 17 00:00:00 2001
From: Anson Huang <Anson.Huang@nxp.com>
Date: Wed, 10 Jun 2020 18:03:02 +0800
Subject: [PATCH 6/9] soc: imx8m: Correct i.MX8MP UID fuse offset

Correct i.MX8MP UID fuse offset according to fuse map:

UID_LOW: 0x420
UID_HIGH: 0x430

Fixes: fc40200ebf82 ("soc: imx: increase build coverage for imx8m soc driver")
Fixes: 18f662a73862 ("soc: imx: Add i.MX8MP SoC driver support")
Signed-off-by: Anson Huang <Anson.Huang@nxp.com>
Reviewed-by: Iuliana Prodan <iuliana.prodan@nxp.com>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 drivers/soc/imx/soc-imx8m.c | 8 ++++++--
 1 file changed, 6 insertions(+), 2 deletions(-)

diff --git a/drivers/soc/imx/soc-imx8m.c b/drivers/soc/imx/soc-imx8m.c
index 7b0759adb47d..0bc831499bd8 100644
--- a/drivers/soc/imx/soc-imx8m.c
+++ b/drivers/soc/imx/soc-imx8m.c
@@ -22,6 +22,8 @@
 #define OCOTP_UID_LOW			0x410
 #define OCOTP_UID_HIGH			0x420
 
+#define IMX8MP_OCOTP_UID_OFFSET		0x10
+
 /* Same as ANADIG_DIGPROG_IMX7D */
 #define ANADIG_DIGPROG_IMX8MM	0x800
 
@@ -87,6 +89,8 @@ static void __init imx8mm_soc_uid(void)
 {
 	void __iomem *ocotp_base;
 	struct device_node *np;
+	u32 offset = of_machine_is_compatible("fsl,imx8mp") ?
+		     IMX8MP_OCOTP_UID_OFFSET : 0;
 
 	np = of_find_compatible_node(NULL, NULL, "fsl,imx8mm-ocotp");
 	if (!np)
@@ -95,9 +99,9 @@ static void __init imx8mm_soc_uid(void)
 	ocotp_base = of_iomap(np, 0);
 	WARN_ON(!ocotp_base);
 
-	soc_uid = readl_relaxed(ocotp_base + OCOTP_UID_HIGH);
+	soc_uid = readl_relaxed(ocotp_base + OCOTP_UID_HIGH + offset);
 	soc_uid <<= 32;
-	soc_uid |= readl_relaxed(ocotp_base + OCOTP_UID_LOW);
+	soc_uid |= readl_relaxed(ocotp_base + OCOTP_UID_LOW + offset);
 
 	iounmap(ocotp_base);
 	of_node_put(np);

From 586745f1598ccf71b0a5a6df2222dee0a865954e Mon Sep 17 00:00:00 2001
From: yu kuai <yukuai3@huawei.com>
Date: Thu, 4 Jun 2020 20:42:06 +0800
Subject: [PATCH 7/9] ARM: imx5: add missing put_device() call in
 imx_suspend_alloc_ocram()

if of_find_device_by_node() succeed, imx_suspend_alloc_ocram() doesn't
have a corresponding put_device(). Thus add a jump target to fix the
exception handling for this function implementation.

Fixes: 1579c7b9fe01 ("ARM: imx53: Set DDR pins to high impedance when in suspend to RAM.")
Signed-off-by: yu kuai <yukuai3@huawei.com>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 arch/arm/mach-imx/pm-imx5.c | 6 ++++--
 1 file changed, 4 insertions(+), 2 deletions(-)

diff --git a/arch/arm/mach-imx/pm-imx5.c b/arch/arm/mach-imx/pm-imx5.c
index f057df813f83..e9962b48e30c 100644
--- a/arch/arm/mach-imx/pm-imx5.c
+++ b/arch/arm/mach-imx/pm-imx5.c
@@ -295,14 +295,14 @@ static int __init imx_suspend_alloc_ocram(
 	if (!ocram_pool) {
 		pr_warn("%s: ocram pool unavailable!\n", __func__);
 		ret = -ENODEV;
-		goto put_node;
+		goto put_device;
 	}
 
 	ocram_base = gen_pool_alloc(ocram_pool, size);
 	if (!ocram_base) {
 		pr_warn("%s: unable to alloc ocram!\n", __func__);
 		ret = -ENOMEM;
-		goto put_node;
+		goto put_device;
 	}
 
 	phys = gen_pool_virt_to_phys(ocram_pool, ocram_base);
@@ -312,6 +312,8 @@ static int __init imx_suspend_alloc_ocram(
 	if (virt_out)
 		*virt_out = virt;
 
+put_device:
+	put_device(&pdev->dev);
 put_node:
 	of_node_put(node);
 

From 4845446036fc9c13f43b54a65c9b757c14f5141b Mon Sep 17 00:00:00 2001
From: yu kuai <yukuai3@huawei.com>
Date: Thu, 4 Jun 2020 20:54:49 +0800
Subject: [PATCH 8/9] ARM: imx6: add missing put_device() call in
 imx6q_suspend_init()

if of_find_device_by_node() succeed, imx6q_suspend_init() doesn't have a
corresponding put_device(). Thus add a jump target to fix the exception
handling for this function implementation.

Signed-off-by: yu kuai <yukuai3@huawei.com>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 arch/arm/mach-imx/pm-imx6.c | 10 ++++++----
 1 file changed, 6 insertions(+), 4 deletions(-)

diff --git a/arch/arm/mach-imx/pm-imx6.c b/arch/arm/mach-imx/pm-imx6.c
index dd34dff13762..40c74b4c4d73 100644
--- a/arch/arm/mach-imx/pm-imx6.c
+++ b/arch/arm/mach-imx/pm-imx6.c
@@ -493,14 +493,14 @@ static int __init imx6q_suspend_init(const struct imx6_pm_socdata *socdata)
 	if (!ocram_pool) {
 		pr_warn("%s: ocram pool unavailable!\n", __func__);
 		ret = -ENODEV;
-		goto put_node;
+		goto put_device;
 	}
 
 	ocram_base = gen_pool_alloc(ocram_pool, MX6Q_SUSPEND_OCRAM_SIZE);
 	if (!ocram_base) {
 		pr_warn("%s: unable to alloc ocram!\n", __func__);
 		ret = -ENOMEM;
-		goto put_node;
+		goto put_device;
 	}
 
 	ocram_pbase = gen_pool_virt_to_phys(ocram_pool, ocram_base);
@@ -523,7 +523,7 @@ static int __init imx6q_suspend_init(const struct imx6_pm_socdata *socdata)
 	ret = imx6_pm_get_base(&pm_info->mmdc_base, socdata->mmdc_compat);
 	if (ret) {
 		pr_warn("%s: failed to get mmdc base %d!\n", __func__, ret);
-		goto put_node;
+		goto put_device;
 	}
 
 	ret = imx6_pm_get_base(&pm_info->src_base, socdata->src_compat);
@@ -570,7 +570,7 @@ static int __init imx6q_suspend_init(const struct imx6_pm_socdata *socdata)
 		&imx6_suspend,
 		MX6Q_SUSPEND_OCRAM_SIZE - sizeof(*pm_info));
 
-	goto put_node;
+	goto put_device;
 
 pl310_cache_map_failed:
 	iounmap(pm_info->gpc_base.vbase);
@@ -580,6 +580,8 @@ iomuxc_map_failed:
 	iounmap(pm_info->src_base.vbase);
 src_map_failed:
 	iounmap(pm_info->mmdc_base.vbase);
+put_device:
+	put_device(&pdev->dev);
 put_node:
 	of_node_put(node);
 

From a721321446432c3899aeca16cc6ddc30422b7f74 Mon Sep 17 00:00:00 2001
From: Peng Fan <peng.fan@nxp.com>
Date: Wed, 24 Jun 2020 14:06:54 +0800
Subject: [PATCH 9/9] soc: imx8m: fix build warning

Fix the build warning with x86_64-randconfig
>> drivers/soc/imx/soc-imx8m.c:150:34: warning: unused variable
>> 'imx8_soc_match' [-Wunused-const-variable]
static const struct of_device_id imx8_soc_match[] = { ^

Fixes: fc40200ebf82 ("soc: imx: increase build coverage for imx8m soc driver")
Reported-by: kernel test robot <lkp@intel.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Signed-off-by: Shawn Guo <shawnguo@kernel.org>
---
 drivers/soc/imx/soc-imx8m.c | 2 +-
 1 file changed, 1 insertion(+), 1 deletion(-)

diff --git a/drivers/soc/imx/soc-imx8m.c b/drivers/soc/imx/soc-imx8m.c
index 0bc831499bd8..cc57a384d74d 100644
--- a/drivers/soc/imx/soc-imx8m.c
+++ b/drivers/soc/imx/soc-imx8m.c
@@ -150,7 +150,7 @@ static const struct imx8_soc_data imx8mp_soc_data = {
 	.soc_revision = imx8mm_soc_revision,
 };
 
-static const struct of_device_id imx8_soc_match[] = {
+static __maybe_unused const struct of_device_id imx8_soc_match[] = {
 	{ .compatible = "fsl,imx8mq", .data = &imx8mq_soc_data, },
 	{ .compatible = "fsl,imx8mm", .data = &imx8mm_soc_data, },
 	{ .compatible = "fsl,imx8mn", .data = &imx8mn_soc_data, },