Second version of this pull request as a small fix to a fix turned
up before Greg pulled it for a cc10001 patch near the top of the tree.
One core fix
* Set updated for a iio kfifo was incorrectly set to false during a failed
update, resulting in atttempts to repeat the failed operation appearing
to succeed.
This time I've decided to list the driver fixes in alphabetical order rather
than 'randomly'.
* axp288_adc - a recent change added a check for valid info masks when
reading channels from consumer drivers.
* bmp280 - temperature compensation was failing to read the tfine value, hence
causing a temperature of 0 to always be returned and incorrect presure
measurements.
* cc10001 - Fix channel number mapping when some channels are reserved for
remote CPUs. Fix an issue with the use of the power-up/power-down register
(basically wrong polarity). Fix an issue due to the missinterpretting the
return value from regulator_get_voltage. Add a delay before the start bit
as recommended for the hardware to avoid data corruption.
* hid pressure - fix channel spec of modfiied, but no modifier (which makes no
sense!)
* hid proximity - fix channel spec of modified, but no modifier (which makes
no sense!). Fix a memory leak in the probe function.
* mcp320x - occasional incorrect readings on dma using spi busses due to
cacheline corruption. Fixed by forcing ___cacheline_aligned for the buffers.
* mma9551 - buffer overrun fix (miss specified maximum length of buffers)
* mma9553 - endian fix on status message. Add an enable element for activity
channel. Input checking for activity period to avoid rather unpredictable
results.
* spmi-vadc - fix an overflow in the output value normalization seen on some
boards.
* st-snesors - oops due to use of a mutex that is not yet initialized during
probe.
* xilinx adc - Some wrong register addresses, a wrong address for vccaux
channel, incorrect scale on VREFP and incorrect sign on VREFN.
-----BEGIN PGP SIGNATURE-----
Version: GnuPG v2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=PiG+
-----END PGP SIGNATURE-----
Merge tag 'iio-fixes-for-4.1a-take2' of git://git.kernel.org/pub/scm/linux/kernel/git/jic23/iio into staging-linus
Jonathan writes:
The usual mixed bag of fixes for IIO in the 4.1 cycle.
Second version of this pull request as a small fix to a fix turned
up before Greg pulled it for a cc10001 patch near the top of the tree.
One core fix
* Set updated for a iio kfifo was incorrectly set to false during a failed
update, resulting in atttempts to repeat the failed operation appearing
to succeed.
This time I've decided to list the driver fixes in alphabetical order rather
than 'randomly'.
* axp288_adc - a recent change added a check for valid info masks when
reading channels from consumer drivers.
* bmp280 - temperature compensation was failing to read the tfine value, hence
causing a temperature of 0 to always be returned and incorrect presure
measurements.
* cc10001 - Fix channel number mapping when some channels are reserved for
remote CPUs. Fix an issue with the use of the power-up/power-down register
(basically wrong polarity). Fix an issue due to the missinterpretting the
return value from regulator_get_voltage. Add a delay before the start bit
as recommended for the hardware to avoid data corruption.
* hid pressure - fix channel spec of modfiied, but no modifier (which makes no
sense!)
* hid proximity - fix channel spec of modified, but no modifier (which makes
no sense!). Fix a memory leak in the probe function.
* mcp320x - occasional incorrect readings on dma using spi busses due to
cacheline corruption. Fixed by forcing ___cacheline_aligned for the buffers.
* mma9551 - buffer overrun fix (miss specified maximum length of buffers)
* mma9553 - endian fix on status message. Add an enable element for activity
channel. Input checking for activity period to avoid rather unpredictable
results.
* spmi-vadc - fix an overflow in the output value normalization seen on some
boards.
* st-snesors - oops due to use of a mutex that is not yet initialized during
probe.
* xilinx adc - Some wrong register addresses, a wrong address for vccaux
channel, incorrect scale on VREFP and incorrect sign on VREFN.
'channels' is allocated via kmemdup and it is never freed.
Use 'indio_dev->channels' directly instead, so that we avoid such
memory leak problem.
Reported-by: Alexey Khoroshilov <khoroshilov@ispras.ru>
Signed-off-by: Fabio Estevam <fabio.estevam@freescale.com>
Reviewed-by: Srinivas Pandruvada <srinivas.pandruvada@linux.intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
According to hardware team there should be some delay after
setting channel number, start mode and before setting START.
Add a one microsecond delay for this purpose.
Fixes: 1664f6a5b0 ("iio: adc: Cosmic Circuits 10001 ADC driver")
Signed-off-by: Naidu Tellapati <naidu.tellapati@imgtec.com>
Signed-off-by: Ezequiel Garcia <ezequiel.garcia@imgtec.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
regulator_get_voltage() returns a non-negative value in case of success,
and a negative error in case of error. Let's fix this.
Fixes: 1664f6a5b0 ("iio: adc: Cosmic Circuits 10001 ADC driver")
Signed-off-by: Naidu Tellapati <naidu.tellapati@imgtec.com>
Signed-off-by: Ezequiel Garcia <ezequiel.garcia@imgtec.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
At present we are incorrectly setting the register to 0x1 to power up
the ADC. Since it is an active high power down register, we need to set
the register to 0x0 to actually power up. Conversely, writing 0x1 to the
register powers it down.
This commit adds a couple of helpers to make the code clearer and then
use them to do the power-up/power-down properly.
Fixes: 1664f6a5b0 ("iio: adc: Cosmic Circuits 10001 ADC driver")
Signed-off-by: Naidu Tellapati <naidu.tellapati@imgtec.com>
Signed-off-by: Ezequiel Garcia <ezequiel.garcia@imgtec.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
New drivers / device support
* st sensors driver, lsm303dlh magnetometer support.
* ltr501 - support ltr301 and ltr559 chips.
New functionality
* IIO_CHAN_INFO_CALIBEMISSIVITY for thermopile sensors.
* kxcjk1013 - make driver operational with external trigger.
* Add iio targets to the tools Makefile.
Cleanups
* st sensors - more helpful error message if device id wrong or irq request
fails, explicitly make the Block Data Update optional rather
than relying on writes to address 0 not doing anything, make interrupt
support optional (Not always wired, and not all devices actually have
an interrupt line.)
* kxcjk-1013 white space additions for readability, add the KXCJ9000 ACPI
id as seen in the wild.
* sx9500 - GPIO reset support, refactor the GPIO interrupt code, add power
management, optimize power usage by powering down when possible, rename
the gpio interrupt pin to be more useful, trivial return path simplification,
trivial formatting fixes.
* isl29018 - move towards ABI compliance with a view to moving this driver
out of staging, add some brackets to ensure code works as expected. Note
there is no actual bug as the condition being tested is always true
(with current devices).
* ltr501 - add regmap support to get caching etc for later patches,
fix a parameter sanity check that always fails (bug introduced
earlier in this series), ACPI enumeration support,
interrupt rate control support, interrupt support in general and
integration time control support, code alignment cleanups.
* mma9553 - a number of little cleanups following a review from Hartmut
after I'd already applied the original driver patch.
* tmp006 - prefix some defines with TMP006 for consistency.
* tsl4531 - cleanup some wrong prefixes, presumably from copy and paste.
* mlx90614 - check for errors in read values, add power management,
add emissivity setting, add device tree binding documentation,
fix a duplicate const warning.
* ti_am335x_adc - refactor the DT parsing into a separate function.
-----BEGIN PGP SIGNATURE-----
Version: GnuPG v2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=wyz7
-----END PGP SIGNATURE-----
Merge tag 'iio-for-v4.2a' of git://git.kernel.org/pub/scm/linux/kernel/git/jic23/iio into staging-next
Jonathan writes:
First round of new drivers, functionality and cleanups for the 4.2 cycle
New drivers / device support
* st sensors driver, lsm303dlh magnetometer support.
* ltr501 - support ltr301 and ltr559 chips.
New functionality
* IIO_CHAN_INFO_CALIBEMISSIVITY for thermopile sensors.
* kxcjk1013 - make driver operational with external trigger.
* Add iio targets to the tools Makefile.
Cleanups
* st sensors - more helpful error message if device id wrong or irq request
fails, explicitly make the Block Data Update optional rather
than relying on writes to address 0 not doing anything, make interrupt
support optional (Not always wired, and not all devices actually have
an interrupt line.)
* kxcjk-1013 white space additions for readability, add the KXCJ9000 ACPI
id as seen in the wild.
* sx9500 - GPIO reset support, refactor the GPIO interrupt code, add power
management, optimize power usage by powering down when possible, rename
the gpio interrupt pin to be more useful, trivial return path simplification,
trivial formatting fixes.
* isl29018 - move towards ABI compliance with a view to moving this driver
out of staging, add some brackets to ensure code works as expected. Note
there is no actual bug as the condition being tested is always true
(with current devices).
* ltr501 - add regmap support to get caching etc for later patches,
fix a parameter sanity check that always fails (bug introduced
earlier in this series), ACPI enumeration support,
interrupt rate control support, interrupt support in general and
integration time control support, code alignment cleanups.
* mma9553 - a number of little cleanups following a review from Hartmut
after I'd already applied the original driver patch.
* tmp006 - prefix some defines with TMP006 for consistency.
* tsl4531 - cleanup some wrong prefixes, presumably from copy and paste.
* mlx90614 - check for errors in read values, add power management,
add emissivity setting, add device tree binding documentation,
fix a duplicate const warning.
* ti_am335x_adc - refactor the DT parsing into a separate function.
When some of the ADC channels are reserved for remote CPUs,
the scan index and the corresponding channel number doesn't
match. This leads to convesion on the incorrect channel during
triggered capture.
Fix this by using a scan index to channel mapping encoded
in the iio_chan_spec for this purpose while starting conversion
on a particular ADC channel in trigger handler.
Also, the channel_map is not really used anywhere but in probe(), so
no need to keep track of it. Remove it from device structure.
While here, add 1 to number of channels to register timestamp channel
with the IIO core.
Fixes: 1664f6a5b0 ("iio: adc: Cosmic Circuits 10001 ADC driver")
Signed-off-by: Naidu Tellapati <naidu.tellapati@imgtec.com>
Signed-off-by: Ezequiel Garcia <ezequiel.garcia@imgtec.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Check whether the allocation of a new kfifo buffer failed or not before
setting the update_needed flag to false. This will make
iio_request_update_kfifo() try to allocate a new buffer the next time a
buffer update is requested.
Signed-off-by: Gabriele Mazzotta <gabriele.mzt@gmail.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Without the cacheline alignment, the readings will occasionally incorrectly
return 0.
Signed-off-by: Michael Welling <mwelling@ieee.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
The LSM303DLH accelerometer/magnetometer has a different
device identification method than using register 0x0f, instead
three registers contain a magic value. We rely on WhoAmI
to be zero for this variant.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
The ST sensors are detected by reading a WhoAmI register and
matching the number found to a sensor name string. To make it
easier to figure out what happens when things go wrong, print
the WhoAmI value and the device name we're trying to match.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Not all sensors support BDU (block data update) and in fact a
bunch of the in-kernel sensor settings do not specify the
BDU address field. Make this optional.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Some sensors such as magnetometers and pressure sensors doesn't
have interrupts at all, and thus no DRDY setting applies. Make
the assignment of an interrupt optional, and do not call
st_sensors_set_drdy_int_pin() if there is no drdy (data ready)
pin specified.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Print a proper error message if we're missing the trigger
IRQ.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Some extra blank lines between if checks don't hurt and improve
readability.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Cc: Bastien Nocera <hadess@hadess.net>
Reviewed-by: Daniel Baluta <daniel.baluta@intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
This id has been seen in the DSDT of the Teclast X98 Air 3G tablet based
on Intel Bay Trail.
Signed-off-by: Antonio Ospite <ao2@ao2.it>
Cc: Bastien Nocera <hadess@hadess.net>
Reviewed-by: Daniel Baluta <daniel.baluta@intel.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Clearly the intent was to error if the value was not 0 or 1.
As implemented we have (A != 0 || A != 1) which is always true
as A is never both 0 and 1 at the same time.
As the autobuilder suggested, && makes more sense for this error
check.
Reported-by: kbuild test robot <fengguang.wu@intel.com>
Acked-by: Kuppuswamy Sathyanarayanan <sathyanarayanan.kuppuswamy@linux.intel.com>
Cc: Daniel Baluta <daniel.baluta@intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Initial value of gpio bitnum is set to -1, but
the variable is declared as unsigned.
Use a positive invalid value for initial gpio
bitnum.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Suggested-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Add mma9553_ prefix to all local functions/declarations.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Suggested-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Use GENMASK instead of BIT or direct value to
define a mask.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Suggested-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Use "GPIO" instead of "gpio" and "ACPI" instead of "acpi".
Includes a couple of small style fixes in comments
(missing full stop, whitespace, paranthesis).
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Suggested-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Use return 0 instead of return ret to mark
clearly the success return path.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Suggested-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
When configuring gpio, we need to read initial values for activity and
step count. This function may fail due to i2c read errors.
Check the error code returned by mma9553_read_activity_stepcnt
and return the appropriate error in gpio config function.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Reported-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
When setting the activity period, the value introduced by
the user in sysfs is not checked for validity.
Add a boundary check so that only allowed values are
reported as successfully written to device.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Reported-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Add an enable channel for activity, so it can also
be polled independently of events or other channels.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Reported-by: Daniel Baluta <daniel.baluta@intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
The mma9551 functions that read/write word arrays from the
device have a limit for the buffer size given by the device
specifications.
Check that the requested buffer length is within required limits
when transferring word arrays. This will prevent buffer overrun
in the mma9551_read/write_*_words functions and also in the
mma9551_transfer call when writing into the MBOX response/request
structure.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Reported-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Refactor code for simplicity and clarity.
This also fixes an endianness issue with the original code.
When reading multiple registers, the received buffer of
16-bytes words is little endian (status, step count). On
big endian machines, casting them to u32 would result in
reversed order in the buffer (step count, status) leading
to incorrect values for step count and activity.
Signed-off-by: Irina Tirdea <irina.tirdea@intel.com>
Reported-by: Hartmut Knaack <knaack.h@gmx.de>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
In SPI mode the transfer buffer is locked with a mutex. However this
mutex is only initilized after the probe, but some transfer needs to
be done in the probe.
To fix this bug we move the mutex initialization at the beginning of
the device probe.
Signed-off-by: Alban Bedel <alban.bedel@avionic-design.de>
Acked-by: Denis Ciocca <denis.ciocca@st.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Added support for Liteon 301 Ambient light sensor. Since
LTR-301 and LTR-501 are register compatible(and even have same
part id), LTR-501 driver has been extended to support both
devices. LTR-501 is similar to LTR-301 in ALS sensing, But the
only difference is, LTR-501 also supports proximity sensing.
LTR-501 - ALS + Proximity combo
LTR-301 - ALS sensor.
Signed-off-by: Kuppuswamy Sathyanarayanan <sathyanarayanan.kuppuswamy@linux.intel.com>
Signed-off-by: Daniel Baluta <daniel.baluta@intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
This device is register compatible with LTR501, with a minor difference for
ALS control register as showed below:
ALS Control register for LTR501:
7 6 5 4 3 2 1 0
+------+------+------+------+------+------+------+------+
| | | | |
| Reserved | Gain | SW | ALS Mode |
| | | Reset| |
+------+------+------+------+------+------+------+------+
ALS Control register for LTR559:
7 6 5 4 3 2 1 0
+------+------+------+------+------+------+------+------+
| | | | |
| Reserved | Gain | SW | ALS |
| | | Reset| Mode |
+------+------+------+------+------+------+------+------+
We handle this difference by introducing ltr501_chip_info.
Datasheet for LTR559 is at:
http://optoelectronics.liteon.com/upload/download/DS86-2013-0003/S_110_LTR-559ALS-01_DS_V1.pdf
Signed-off-by: Daniel Baluta <daniel.baluta@intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
The VREFN channel is bipolar, not unipolar. Small negative values do
occur (e.g., -1mV), and unsigned conversion maps them incorrectly to
large positive values (about +1V), so fix this.
Signed-off-by: Thomas Betker <thomas.betker@rohde-schwarz.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
The scaling factor for VREFP is 3.0/4096, not 1.0/4096; fix this to get
correct readings.
Signed-off-by: Thomas Betker <thomas.betker@rohde-schwarz.com>
Cc: <stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
For the "vccaux" channel, read the VCCAUX register, not VCCINT.
Signed-off-by: Thomas Betker <thomas.betker@rohde-schwarz.com>
Cc: <stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Define the register addresses for MIN_VCCPINT, MIN_VCCPAUX, MIN_VCCO_DDR
correctly.
Signed-off-by: Thomas Betker <thomas.betker@rohde-schwarz.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Added ACPI enumeration support for LTR501 chip.
Signed-off-by: Kuppuswamy Sathyanarayanan <sathyanarayanan.kuppuswamy@linux.intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Added rate control support for ALS and proximity
threshold interrupts.Also, Added support to modify
and read ALS & proximity sensor sampling frequency.
LTR-501 supports interrupt rate control using persistence
register settings. Writing <n> to persistence register
would generate interrupt only if there are <n> consecutive
data values outside the threshold range.
Since we don't have any existing ABI's to directly
control the persistence register count, we have implemented
the rate control using IIO_EV_INFO_PERIOD. _period event
attribute represents the amount of time in seconds an
event should be true for the device to generate the
interrupt. So using _period value and device frequency,
persistence count is calculated in driver using following
logic.
count = period / measurement_rate
If the given period is not a multiple of measurement rate then
we round up the value to next multiple.
This patch also handles change to persistence count whenever
there is change in frequency.
Signed-off-by: Kuppuswamy Sathyanarayanan <sathyanarayanan.kuppuswamy@linux.intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
This patch adds interrupt support for Liteon 501 chip.
Interrupt will be generated whenever ALS or proximity
data exceeds values given in upper and lower threshold
register settings.
Signed-off-by: Kuppuswamy Sathyanarayanan <sathyanarayanan.kuppuswamy@linux.intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Added support to modify and read ALS integration time.
Signed-off-by: Kuppuswamy Sathyanarayanan <sathyanarayanan.kuppuswamy@linux.intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Fix "null" in the raw attribute and scan elements.
Signed-off-by: Srinivas Pandruvada <srinivas.pandruvada@linux.intel.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
If a GPIO reset pin is listed in ACPI or Device Tree, use it to reset
the device on initialization.
Signed-off-by: Vlad Dogaru <vlad.dogaru@intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
In the interest of lowering power usage, we only activate the proximity
channels and interrupts that we are currently using.
For raw reads, we activate the corresponding channel and the data ready
interrupt and wait for the interrupt to trigger. If no interrupt is
available, we wait for the documented scan period, as specified in the
datasheet.
The following types of usage patterns may overlap:
* raw proximity reads (need a single data ready interrupt)
* trigger usage (needs data ready interrupts as long as active)
* proximity events (need near/far interrupts)
* triggered buffer reads (don't need any interrupts, but are usually
coupled with our own trigger.
To mitigate all possible patterns, we implement usage counting for all
the resources used: data ready interrupts, near/far interrupts and
individual channels.
The device enters sleep mode as documented in the data sheet when its
buffer, trigger and events are disabled, and no raw reads are currently
running.
Because of this new usage pattern, it is important that we give the
device a chance to perform an initial compensation for all its channels
at probe time.
Signed-off-by: Vlad Dogaru <vlad.dogaru@intel.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>